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MID MAIN JET & TEMP

Started by bugcool, July 01, 2007, 04:26:57 PM

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bugcool

G'DAY guys, im getting a lean spot between 5 & 6.3k but only at night, day time its prob still there but i can't feel it. The temp by day is 63 ish & night is 46f  my jets are 20 , 62.5 , 137 with float hight 2mm above gasket & needle is 4th down , air is by k&n dropin with stock exhast. So i was going to put in a 65 mid jet, would this be going to far for a mid jet.

bugcool

  you could try it , just see what it dose.    BTW do you allways talk to yourself .

Wrecent_Wryder

Everyone's been in enough "spirited" jetting discussions at this point that they may be a little tired.

Personally, I'd guess that you're fine with the 62.5 mid with your setup... it worked beautifully for mine when I was running the K&N lunchbox with the stock exhaust. Of course, others will disagree.

Are you sure it's lean? A "stutter" in that RPM range is more often associated with being too rich. Usually, lean "surge" shows up first between 7-8k.

Don't discount the effect of the mixture screws- I shouldn't have. A careful half-turn one way or the other will probably change things enough to tell whether it's better or worse.
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scratch

Two other words used in seat-of-the-pants tuning are "hesitation" (lean) and "bogging" (rich).
The motorcycle is no longer the hobby, the skill has become the hobby.

Power does not compare to skill.  What good is power without the skill to use it?

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good judgement trumps good skills every time.

bugcool

it feels like its running out of fuel.  and it got better not fixed but better when i put the restrictor ring in so that richend it a bit.

bugcool

 Yesterday i turned the mix screw out 4 turns, its a lot better but not fixed,  so that ring in the k&n and the 4 turns made it richer & it feels 80% better so im going to try a 65 mid jet & put the other stuff back how it was.

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